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4.16kV 및 6.6kV 전동기 고정자 권선의 절연열화 판정기준
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  • 4.16kV 및 6.6kV 전동기 고정자 권선의 절연열화 판정기준
저자명
김희동,Kim. Hee-Dong
간행물명
전기학회논문지= The Transactions of the Korean Institute of Electrical Engineers
권/호정보
2009년|58권 4호|pp.788-794 (7 pages)
발행정보
대한전기학회
파일정보
정기간행물|
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기타
이 논문은 한국과학기술정보연구원과 논문 연계를 통해 무료로 제공되는 원문입니다.
서지반출

기타언어초록

To assess the condition of stator insulation, nondestructive tests were performed on twenty five coil groups and twenty six motors. The stator windings has nominal ratings of 6.6kV and are classified into five coil groups ;one group with healthy insulation and four groups with four different types of artificial defects. After completing nondestructive tests, the AC voltage applied to the stator windings was gradually increasing until insulation failure in order to obtain the breakdown voltage. No.1, No.2 and No.6 of 6.6kV motors failed near rated voltage of 14kV, 8.7kV and 14kV, respectively. The breakdown voltage of three motors was lower that expected for good quality coils(14.2kV) in 6.6kV motors. No.3 and No.6 of 4.16kV motors failed near rated voltage of 5.6kV and 4.2kV, respectively. Almost all of failures were located in a line-end coil at the exit from the core slot. The breakdown voltages and the types of defects showed strong relation to the stator insulation tests such as in the case of AC current, dissipation factor(tan${delta}$) and partial discharge magnitude.